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Not quite The Archers or Neighbours but random jottings just to keep you posted


This space awaits _YOUR_ contribution!

Please let me know what you have been doing, especially if it embarrasses you!


August 2010


The second Bank Holiday Weekend must be the busiest that we have ever had, to the extent
that our resources were stretched out to the limit! On the Sunday, we supported two
social events in parallel, the Families' Day run by the White Horse leisure park and also
the village fete at Steeple Ashton where we were in competition for giving rides with the
dray and shire horses from Wadworth's Brewery. Nevertheless, a good time was had by all.*****

On the Monday we met at Nev's for the steam-up with the Teddy Bear theme, where anybody who turned
up holding a Teddy Bear got the first ride free; the oldest claimant being 92 years of age,
but now shamefacedly admitting to using someone else's Teddy Bear, after noticing that the blog had
originally classed him as being in his 80s!


*****Which reminds me of the old chestnut as to what is the difference between a Cavalry
Charger and a Brewer's Horse?

Well, apparently the former darts in the fray ...


Saturday 14th August saw us at what has been our major event for the past few years,
the Seend fete. A rainy day seemed to discourage the children from attending, but a
good turnout for club members, nevertheless.
Tom Buckland had brought along his 57XX but had to withdraw it from service after it
became apparent that the boiler wasn't being filled and once again we turned to Mike
Richardson with his Polly to provide the steam hauling after Nev's Class 20 got
the event moving for us

The rain kept off for most of the afternoon, apart from an occasional slight drizzle, but
at about 15:30 the skies opened. Mirabile dictu*****, the queue of those wanting a ride then grew!


***** "Quidquid Latine dictum sit, altum videtur", perhaps?


... and another bulletin from the Mill Lane surgery of Dr.Boulton ...

Our Honorary Treasurer, Denis Hurn is the owner of a small 0-4-0 Maxitrack electric
shunter locomotive. Denis has had this loco for many years and it would never pull any
load in the forward direction without the gearing slipping or more correctly the gears
coming out of mesh. So Denis always(very sensibly!) drove it backwards. When he told me about
the problem I suggested that If he let me have the machine for a few days that I could take
a look at it. The drive from the electric motor was found to be through four gears, two of
which were 'idlers' on the same shaft. The gear teeth were only just engaging at the tips of
the teeth so that when the motor had a load on it the torque caused a slight movement which
forced the gear teeth apart thus loosing traction to the wheels. This was cured by packing
out the motor with half a dozen penny washers which ensured the full engagement of the gear
teeth in the drive chain. Whilst I was at it - I re-secured one of the driving wheels (which
was loose) to the axle, locktighted the two idler gears together and secured the gear on the
motor shaft with a fresh grub screw. Tested on the track - and found serviceable.


July 2010


... from our intrepid reporter, David Clarke ...

On Monday the new toilet building arrived and has been put up on the base in the last couple of days. We had an old toilet it was called the Hedge. We now have to fit it out. Will we get bogged down with all the work?

(Ed's note ... despite being renowned for my toilet sense of humour, I won't try to upstage David. But ... what can that trapdoor half way up the wall possibly be for? ... Answers on postcards only, please, to this address!)



... the next bulletin from the Mill Lane surgery of Dr.Boulton ...

Just done another £80 birthday party on the GBR for the village hall.
Chairman Duncan from the ME Society brought me a small 5" gauge 0-4-0 Maxi-Track
electric shunter to fix whilst we were at it!

Apparently he bought the kit a few years ago and never got it to run. It has a
20 amp 4QD card, reversing switch and a braking switch. All the braking switch
does (according to the wiring diagram) is to remove the power supply and join both
wires of the motor together. When I looked at the reversing switch
(double pole , centre off) I was immediately suspicious because there were no cross
over wires which reverse the polarity when selected. The output to the motor is taken
from the centre terminals. Anyway I connected the motor directly to the 4QD card outputs
and it worked OK. This proved the 4QD controller, speed control rheostat and the motor.
After that it was just a question of re-wiring the reversing switch properly. We tested it
on the track and it is very lively - the braking switch is very severe and in my opinion
should only be used in an emergency because it might cause the gear train to strip off a tooth!

During the testing the new wooden (Lottery Funded) toilet building arrived from the timber
shop together with a team of 3 blokes to erect it. So when they had their tea break we let
them all have a go at driving Duncan's electric loco.

(Ed's note ... presumably the testing was at the Club's site. Surely Bulkington is not so far
out in the sticks as to find the arrival of a modern toilet facility to be something to comment on? :-) )


Saturday 17th July and a hot sunny afternoon after a dull morning saw a very successful visit
to Nev's Great Bulkington Railway, raising money for the Air Ambulance and the Dorothy House
Foundation. I've been at Nev's when there has been a huge public turnout, and I've been at
Nev's when there's been a lot of engines, but never both at the same time! I have to apologise
to young Ben for not letting him have his training session in the signal box, as had been promised,
and using his services all afternoon as a ticket seller!

We were very pleased to be host to a couple of visiting engines from our neighbouring club, the
North Wilts bods, whose Prairie Tank did sterling service all afternoon on passenger hauling.


Saturday 10th July and we did a successful fete at Bratton where the theme was pirates, although
this was unbeknown to us until we arrrived. It was another blistering hot sunny day.
This is the last of the weekend-in, weekend-out series of fetes that has kept us from our own lathes
and milling machines during the past 6 weeks. We now look forward to our regular venue at Seend on the 14th August


Friday 9th July and a surprise evening fete and barbeque at the primary school at Westbury Leigh
and an unscheduled outing for the portable track, supported by Dennis's battery 0-4-0 and Mike's
recently-completed Polly. Mike is giving us sterling service with his locomotive at many of our recent fete visits.
Your scribe knew nothing about this fete, and does not to this day, other than it took place and
was set up by the cognoscenti of the WWSME Mafia at very short notice!


June 2010


26th June saw us at a new venue, the Church Fete at Great Cheverell.

An extremely hot sunny day, with no shade on offer, and an excellent cake stall,
(whose delights were denied to your scribe following an exercise-book-down-the-back-of-the-trousers
episode with the Diabetic Nurse at the 6-monthly check-up!),
but once again a very poor day for us for income as we barely covered our costs of attending.

We had just set up the station areas when the band (for want of a better word!) struck up
on the articulated lorry provided as the platform. So unpleasant did we find the music (again, for
want of a better word!) that we upped sticks and moved the station to the other end of the track.

John and Dennis had waited at Westbury for the passage of the King Edward I steam-hauled excursion
but on getting a message that it had failed at Newbury, then came on along to Great Cheverell.
Gareth, Mike and Derek were chewing grass stalks leaning on a farm gate at the fete site awaiting
this same steam-hauled special, which finally came through 3/4 of an hour late.


Your webmaster completed the main loop of his ground-level 16mm track and held an impromptu
garden meeting on the 24th June to test it. All ran well apart from Mike's 6-coupled steamer
which would not restart on the combined curve and gradient at Miser's Meander.
Miser's? Assumed because the gauge was too tight.***** Apun my word!

Apologies to those members of the 16mm group whom I did not invite because I did not have contact details for you.


*****Ed's note :- Subsequently found to be a slope of 1 in 20, as against the rest of the garden with 1 in 80


19th June saw us at a new venue, the Strawberry Fayre at Fitzmaurice Primary School in Bradford-on-Avon
A pleasant sunny day with some cold winds, and a tremendous variety of stalls provided by the school,
but a very poor day for us for income as we barely covered our costs of attending.


The village social in Bratton had as its theme this year Steam Engines, and the 16mm portable track was
taken there as part of the entertainments. By all accounts, our club members were wined and dined
in excelsis by the grateful villagers.


Maundy Money?

The habit of the monarch to distribute Maundy Money on Maundy Thursday was emulated by John driving back
from the Monkton Farleigh fete - some items were lifted by the slipstream and broadcast onto the surrounding
grass verges. Luckily, Mike and Clare were following close behind and were able to reclaim the truanting
items. We have now covered the trailer with fish netting to prevent a re-occurence.


Monkton Farleigh fete on the 12th June gave us mixed feelings. The weather was good and the physical
geography was good, with the portable track being almost level and laid along the entrance road into
the Manor House, but with the car park being in the Orchard immediately as you came through the main
gate, most of the visitors did not pass the railway, and could not see it from the fete, because
the drive is hidden behind a row of bushes, so the day's takings did not reflect the densely packed
front lawn of the Manor House that was the very successful village fete.
We ran pushme-pullyou with Des Clarke's Sweet Pea at one end, and Mike Richardson's Polly at t'other. Des
had steaming problems with a clinkering grate, requiring the occasional intervention of Dennis Hurn's
battery electric whilst the Sweet Pea's marine boiler was shaken out and re-fired.


FRUSTRATION IS .....

Pulling a nail from a spare piece of wood. Despite your vice-like grip,
the pliers slip off, your elbow travels back at high speed and bruises
into the bench vice. You drop the piece of wood which lands on your
favourite scribing tool***** which just happened to be half on and half off
the bench. The scriber is launched into a roly-poly base-over-apex flight
across to the nether regions of the workshop where it takes 3 hours of
moving the scrap about to recover it.

It would have been quicker all-told to have gone down to B&Q and
purchased a new piece of wood to suit the job in hand, which time and
inconvenience you were trying to avoid in the first place!

***** Even though you've got 3 other scribers that would do any job
that comes along, it doesn't feel "right" unless you're using your favourite.


The Gala Day on the 5th June was a great success, with blisteringly hot sunny weather
Talk about Flaming June!
It is hard to believe that it is already one year since our Grand Opening last year!


May 2010


Had a good day on 31st May at the Lions Fun Day in Bradford-on-Avon. Mostly overcast with
only a couple of drops of rain. Sterling service given by Mike Richardson's new Polly
steam engine and with Peter Whisstock's Dad's 0-4-0 Steam Dock Shunter
This year we were better sited up the bowling green end, right by the classic car
collection. We only had to give one free ride to calm the tantrum of a young lass
who did not want to get off!


Pat Clarke (Mrs) for the England Cricket Team! ...

At the Woody Bay gathering, a guest was running his live steamer on our portable
16mm layout, and took the corner too fast, resulting in the locomotive careering off
the trestle and into the capable hands of Pat Clarke who unfortunately sustained
an injury necessitating the attention of the boys-in-green.
Pat, award yourself the C.D.M. (Cadbury's Dairy Milk)

... but more importantly, no damage to the engine!


The 16mm group have completed the 45mm third rail around the outside of the 16mm portable track, so any of you with LGB stock that (in theory!) belongs to your children or grandchildren can now run this at the meetings.


On the (first!) May Bank Holiday Monday, we took the other (5" & 3 1/2") portable track along to Christ Church School in Bradford-on-Avon and had a very good day out, despite a JCB being parked across the access to the portable track. This caused a delay of 1 1/2 hours and a lot of phoning around of a Saturday morning to sort out, and by the time that we got to the school grounds, all the stakes and orange plastic fencing that had been provided had been purloined by other stands. A quick recourse to our red-and-white plastic tape and we soon had our reserved area protected.

We did very well out of the day, and perhaps in the future we should try to get a pitch that is in the middle of all the other stalls in the same way. That is now two successful fetes at the start of the season and John Drewett is to be congratulated on taking up the reins as fete organiser after the sad loss last year Of Graham Myatt.


After some discussion with the new owners of the Westbury Leisure Park (who quite understandably wish to maximise their revenue from their new investment), it has been resolved that there will not now be any changes to the club's 5" and 3 1/2" fixed track.

... And did you know that the thickness of metal used to create the 3 1/2" track had been cunningly chosen such that (brave?) owners of coarse scale O gauge trains can run them in the remaining gap? This, of course, includes aficionados of the 16mm narrow gauge pursuit. But, talking of pursuit, you'd better ensure that there isn't a 5" gauge Simplex coming up behind you!


... and now a report from the Mill Lane surgery of Dr.Boulton ...

Whilst I have been waiting for Dan Jeavons to produce the body for my new Class 20 electric loco. The bogies are finished and painted. I spent a couple of days earlier this week sorting out the valve event problems on Chairman Duncan's Polly Loco. Everything was very tight and stiff - The wheels needed a strap wrench to turn them. He had the back axle (complete with valve eccentrics) fitted in back to front so that the R/H valve events were occurring on the L/H cylinder. Highly confusing! Lots of theories and detective work! He also had fitted one of the eccentrics in the wrong position on the axle. Once we got it sorted out and timed correctly I ran it in on air for several hours with loads of oil. Duncan has now taken it away for several more hours of air powered running in prior to fitting the boiler. Should be on the track soon! Later in in the week (as I was in full up-to-date valve practice) with valve gear - I spent a day with Andy Coultiss fixing the timing on his big 0-8-2 banking engine. We took the boiler and smoke box off to access the cylinders and valve gear which are located under the smoke box. During this operation of course we damaged the gasket and had to make a new one - which also involved making a gasket punch for the 6BA holding down bolts. Needless to say several odd bits and pieces required re-manufacturing - I am pleased to report that the job is now about 90% finished. Should be on the track soon!